DO王社平1,2,李磊1,杨亚红1,郑阳光1,张雅静1,张欣蓓1(1.西安建筑科技大学环境与市政工程学院,陕西西安710055;2.西安市政设计研究院有限公司,陕西西安710068)以实际污水处理厂的沉砂池出水为研究对象,在微孔曝气氧化沟中试装置中进行了低溶解氧浓度和污泥微膨胀条件下去除污染物的试验并分析了节能效果。通过电动阀控制曝气量,使曝气区的DO维持在0.5~0.9mg/L之间,SVI值为150~250mL/g,即污泥处于丝状菌微膨胀状态,可以节省曝气量约50%,且对COD、NH3-N、TN和TP的平均去除率分别达到92.5%、99.1%、82.1%和96.2%,出水SS平均值小于10mg/L,满足《城镇污水处理厂污染物排放标准》中一级A的要求,实现了低溶解氧浓度和污泥微膨胀状态下的运行与高效脱氮除磷。污水处理厂;氧化沟;低溶解氧;污泥微膨胀;节能效果X703A1000-4602201221-0005-04EffectofLowDOinPilot-scaleOxidationDitchonPollutantRemovalandEnergySavingWANGShe-ping12LILei1YANGYa-hong1ZHENGYang-guang1ZHANGYa-jing1ZHANGXin-bei11.SchoolofEnvironmentalandMunicipalEngineeringXi’anUniversityofArchitectureandTechnologyXi’an710055China2.Xi’anMunicipalEngineeringDesignandResearchInstituteXi’an710068ChinaAbstractTheactualeffluentfromgritchamberofawastewatertreatmentplantwasusedtoinves-tigatethepollutantremovalefficiencyandenergysavingeffectinapilot-scalemicroporousaerationoxida-tionditchunderconditionsoflowDOandlimitedfilamentoussludgebulking.TheDOconcentrationwasmaintainedbetween0.5mg/Land0.9mg/LandSVIvaluerangedbetween150mL/gto250mL/gwhichcouldcauselimitedfilamentoussludgebulkingandaerationreductionof50%.Theaverageremov-alratesofCODNH3-NTNandTPwere92.5%99.1%82.1%and96.2%respectively.Theef-fluentSSwaslessthan10mg/L.TheeffluentqualitymetthefirstlevelAcriteriaspecifiedinDischargeStandardofPollutantsforMunicipalWastewaterTreatmentPlantGB18918-2002.KeywordswastewatertreatmentplantoxidationditchlowDOlimitedsludgebulkingenergysavingeffect2009ZX07317-009。1。SVI150mL/g·5·第28卷第21期2012年11月中国给水排水CHINAWATER&WASTEWATERVol.28No.21Nov.20122。DO0.5~0.9mg/LSVI150~250mL/g。1试验装置与方法1.11。2.10m×0.70m1.60m2.35m326.25m3。、1∶7∶4。200mm2。14.15h15d50%~60%。1Fig.1Flowchartofpilot-scalemicroporousaerationoxidationditch1.2。1。1Tab.1Rawwastewatercharacteristicsmg·L-1COD300~700536TKN50~8061.7NH3-N20~5040.7TP4.5~9.56.9PO3-4-P2.5~43.21.3COD、TKN、TP、NO-3-N、NH3-N、PO3-4-P、MLSS3DOHachADV。2结果与讨论2.1DODOMLSSSVI。SVIMLSSSV70%~95%83%MLSS3.5~4.5g/L4.05g/LSVI170~250mL/g200mL/g。。SS150~550mg/L379mg/LSS<10mg/L5mg/L50%~60%。DOSS。、SS。2.22.2.1COD、COD53638.3mg/LCODA92.5%。DOCOD。4COD。2.2.2NH3-NTNDO、DO。、NH3-N40.70.38mg/LNH3-NA99.1%。DONH3-N。Hanaki5DO1DO0.5mg/L·6·第28卷第21期中国给水排水.watergasheat.com。2。0.094gNH3-N/gVSS·d50dDO0.134gNH3-N/gVSS·d40%NH3-N。0.095gNO-2-N/gVSS·d0.16gNO-2-N/gVSS·d。。2Fig.2Variationsofnitrificationrateduringsludgebulking、TNTN61.7mg/LTN<14mg/L10.24mg/LA82.1%。TN13.96mg/L7.82mg/L72%86%。TN。6∶57∶46。0.347gNO-3-N/gVSS·d0.065gNO-3-N/gVSS·d0.134gNO-3-N/gVSS·d0.049gNO-3-N/gVSS·dTN。2.2.3TPDO2mg/LDO。、TP6.920.26mg/L96.2%。DOTP0.05~0.46mg/LA。TNNO-3-NNO-3-NDOA/OTP。0.141、0.107gPO3-4-P/gVSS·d。DOTP。2.32.3.1。123。1.15m30.2、0.61.0m。·7·.watergasheat.com王社平,等:低DO浓度下氧化沟的除污及节能效果分析第28卷第21期3Fig.3Measurementsectionandaveragevelocitydistributionofsections30.14~0.17m/s0.15m/s。。≥0.3m/s、≥0.1m/s≥0.1m/s0.15m/s。。≥0.15m/s。2.3.2。DO0.5~0.9mg/L42m3/hDO2mg/L88m3/h50%。3结论①DO0.5~0.9mg/LSVI150~250mL/g50%。②COD、NH3-N、TNTP92.5%、99.1%、82.1%96.2%SS10mg/L《》A。③、。④0.15m/s≥0.15m/s。⑤DO0.5~0.9mg/L。1.SBRJ.200420840-42.2KruitJHulsbeekJVisserA.BulkingsludgesolvedJ.WaterSciTechnol2002461/2457-464.3.4M.2002.4.、J.200829123342-3347.5HanakiKWantswinCOhgakiS.Nitrificationatlowlev-elsofdissolvedoxygenwithandwithoutorganicloadinginsuspended-growthreactorJ.WaterSciTechnol1990243297-301.6ZhaoHWMavinicDSOldhamKW.Controllingfac-torsforsimultaneousnitrificationanddenitrificationinatwo-stageintermittentaerationprocesstreatingdomesticsewageJ.WaterRes1999334961-970.1963-。E-mailwsp901@vip.sina.com2012-07-12·8·第28卷第21期中国给水排水.watergasheat.com