短程生物脱氮与同步除磷的中试研究徐晓宇

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38    Vol.32 No.11 2006徐晓宇 杨殿海(, 200092)   交互式反应器运行倒置A2/O处理低碳高氮城市污水,在其好氧段通过控制DO为0.5~1mg/L,进行短程硝化研究。结果表明:在总HRT为10h条件下,经过1个月左右稳定运行后,亚硝氮的累积率可以达到50%以上,最高达到75%左右,而且反应器对总氮的去除也有明显改善,出水总氮平均在10mg/L左右。亚硝酸盐在预缺氧区和缺氧区的反硝化反应较为彻底,进入厌氧池后不会对厌氧段生物释磷产生抑制。但是,低氧条件下的短程硝化过程会导致污泥沉降性能恶化,容易产生污泥膨胀,不过通过控制好氧末端的后曝气提高DO可以改善污泥的性状。 短程硝化 低碳高氮磷污水 交互式反应器 脱氮除磷Pilot-plantresearchonshort-termdenitrificationandsimultaneousPremovalXuXiao-yu,YangDian-hai(StateKeyLabofPollutionControlandResourceReuse,TongjiUniversity,Shanghai200092,China)Abstract:InvertedA2/Oprocessinaninteractivereactorwasconductedtotreatmunicipalwastewaterwithhighnitrogenandlowcarboncontents.TheDOlevelattheaerobicsectionwascontrolledinrangeof0.5to1.0mg/Ltoinvestigatetheshort-termnitrification.Afteraboutone-monthsteadyoperation,average50%andmaximum75%ofnitriteaccucmulationwereobtainedundertotalretentiontimeof10hours.Alsotheremovaloftotalnitrogeninthereactorwasimprovedevidently;theaverageTNcontentintheeffluentwas10mg/L.Thedenitrificationofnitriteprogressedstronglyatthepre-anoxiaandanoxiazone,nodepressiontothebiologicalphosphorusreleaseintheanoxiasectioncouldbefounded.Buthowever,thelowoxygenconditionforshort-termnitrificationdeterioratedthesettlementfeatureofthesludge.Sludgebulkingwasobserved,butitcouldbeprotectedbywayofenrichedaerationattheendoftheaerationsectionofthereactor.TheincreasedDOlevelcanimprovethesedimentationfeatureofthesludge.Keywords:Short-termnitrification;Wastewaterwithhighnitrogenandphosphorusandlowcarboncontents;Interactivereactor;Nitrogenandphosphorusremoval  ,,、pH、DO。DelftSHARON30~35℃(863)(2002AA601023)。[1]。,pH8[2]。:pH7.490%,pH7.4~8.3[3]。30℃pH8,,DO。HannakiK[4],25℃,DOI:牨牥牨牫牱牳牴牤jcnkiwwe牨牴牰牬牪牥牥牰牨牨牥牨牥 Vol.32 No.11 200639   DO(0.5mg/L),,。Ruiz[5],DO0.7mg/L。,,,,,,。,DO,,,。1 1.1 /,,6.3m,2m,3m,37m3,100m3/d。1,1。1#~3#,4#~6#。:①,,;②,,,;③,,。1   /m/m30.7×1×32.11.94×1×35.822×1×366.3×1×318.91.6×1×34.82.85×212.751.2 ,2,、1 2 3 45 6 71 /2 pHCODCr/mg/LSS/mg/LNH3-N/mg/LTN/mg/LTP/mg/L7~8100~2006020~3030~402~3,。1.3 CODCr、NO-2-N、NO-3-N、NH3-N、TN、TPMLSS,[6];DOWTWOxi330iDO;pHWTWpH330ipH。1.4 A2/O,20058,A2/O,30%2#,70%3#,1#,。:4.2m3/h;MLSS2200mg/L;25d,100%。20059~11,:1~20d,DO2mg/L,;21d,DO0.5~1mg/L,A2/O。,。2 ,22~27℃。20d,A2/O。2,,1mg/L,15mg/L,30%,。21~60d,(4#)DO,0.5~1mg/L,40    Vol.32 No.11 2006,A2/O,3。3,1mg/L,,DO,,DO;,,,DO,,,DO,。36d,50%,,50%,。:,。10d,,,,15mg/L,50%;,,10mg/L,65%。:,,。,。A2/O,,3#。1#2#:1#,;2#30%。4,2#,,3#1mg/L,,。5,,,30%,,,。,。,DO,[7]。[8],。21~33d,,(5#)DO,(6), Vol.32 No.11 200641   SVI170mL/g,,;34d,DO2~3mg/L,,,SVI100mL/g。:DO,,SVI,。6 SVI3 (1)A2/ODO0.5~1mg/L,,,,,15%。(2),1mg/L,,。(3),,DO,,。(4),、,。参考文献1 ,,,./Ι..,2004,24(5):762~7692 ,./.,2001,21(1):79~833 ,,..,1999,25(7):37~394 HanakiK,WantawinC,OhgakiS.etal.Nitrificationatlowlevelsofdissolvedoxygenwithandwithoutorganicloadinginasuspendedgrowthreator.WatRes,1990,24(3):297~3025 RuizG,JeisonD,ChamyR.Nitrificationwithhighnitriteaccumulationforthetreatmentofwastewaterwithhighammoniaconcentration.WatRes,2003,37:1371~13776 《》..3.:,19897 .:[].:,20038 ,,,..,2003,19(7):7~11  &:2000921239309#E-mail:xxy1002@163.com:2006-05-24管 井 修 复 的 常 用 方 法  ,、、,,,。,,,,,,。:(1),。(2),,,:①、、、;②;③、;④。  (3),、,:①,,;②,,;③,、,d-d≥50mm。1m,。,。(4)24d,,,。(山西关铝股份有限公司 杜高民)

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