高浓度有机废水大型厌氧反应器的调试和起动运行李锡英

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李锡英 刘 戈 杨沂凤(,330029) 介绍了高浓度有机废水大型厌氧反应器的调试和起动运行的全过程。采用处理同类废水中温发酵的厌氧污泥作种泥,满罐低浓度接种。通过逐步提高负荷和升温,培养和驯化出足够数量高温发酵的活性污泥,60d以内就能正常生产运行,达到设计所预期的目标。较常规起动方法可缩短时间1倍以上。 大型厌氧反应器 高浓度有机废水 调试 起动运行1 ,。、、、CODCr90%,———。1t500m3,CODCr4×104~5×104mgL,SS2.5×104mgL。CODCr3×103mgL,SS2.5×103mgL,6×103m360%。,。,。2 ,。(USR)(SSB)21,USR,。(CODCr)(SS)。:(1)50d,,,,,,CODCr92%。(2),,,SS88%。CODCrSS,,,,。3 t,2,。1500m3,2,USR,,1000m3;SSB,、。,:(1),;(2),;(3)USRSSBUSR,();(4);(5)。4 、、、。,。,,1000m3,。4.1 复合厌氧反应器试水试压检漏和联动试机,;;32   20024202DOI:10.13205/j.hjgc.2002.02.011。,——————,24h,,,2,24h,,5%。,USR,,、、、,,。4.2 接种、启动,35℃,。、35℃,SS1.2×104mgL,pH7.6,90m3。20m3,,2d,,3~5d,。4.3 污泥培养,,,。CODCr7kgm3,0.5kgm3·d,--,5,2m3,。,,0.5~1kgm·d。:(1)pH。、、pH,pH6.8~7.8。(2)CODCr。CODCr80%,60%。(3)。,1~1.5℃,55℃。(4)pH。CODCr,,50%。4.4 稳态运行50d,,,20,18~20m3。3m30kgm,55±2℃,CODCr90%,4~6m3m3·d,60%,。5000~6000m3。5 (1),,。,。(2),,。(3),,0.5~1kgm3·d。(4)、,55℃。(5)pH、CODCr。,、,60d,1。1 ..:,1998.2 ..,1999.17(1).3 ..,2000.20(1). ,,194610,1968,。,、,、。2001-09-2133   20024202Abstract ThreedegradablestrainsW1,W2,Y3isolatedfromcontaminatedsoilusingawastewaterfrompyrethroidandheterocyclicpesticidesproductsfactoryasasoleenergyandcarbonsource,weremixedandculturedtoobtainaLivingLiquorMicroorganisms(LLMO).Thebacteriaquicklyformedathinfilmonthecarriers.CODCrremovalratesof24.8%,43.5%and53.4%wereachievedundertheconditionof6810,3130and1890CODCrmgLfeed,respectively,aftertheoperationofa24-hperiod.Utilizinganadaptedactivatedsludgeasacontrol-experiment,theCODCrremovalratewasonly56.7%overthecourseof24-hofprocess,indicatingthatitispossibletotreatthissortofwastewaterbysomeeffectivemicrobialfilms.Keywords degradablestrains,bacterialfilmsandpesticidewastewaterTREATMENTOFCATTLEWASTEWATERWITHSINGLESTAGEANDTWO-STAGESEQUENCINGBATCHREACTORLiXiujin(23)…………………………………………………………………………Abstract ThecharacteristicsofSequencingBatchReactor(SBR)wasintroduced.Thewastewaterfromacattleranchwastreatedwiththesingle-stageandtwo-stageSBR,respectively.Itwasfoundthatthesingle-stageSBRwascapableofachievingsatisfactorycarbon,solidsandnitrogenremovalefficiencyandgoodeffluentquality.Buttwo-stageSBRprovedtobemoreeffectiveintermsoftreatmentefficiencyandammoniaconversionascomparedwithsingle-stageSBRsystem.Keywords treatment,wastewater,cattleranchandsequencingbatchreactorTREATMENTOFFOODSTUFFFLAVORINGWASTEWATERBYABR-SBRPROCESSChengKaiyingetal(26)………………………………………………………………………………………………………………………Abstract TheprocessofABR-SBRwasselectedtotreatfoodstuffflavoringwastewaterinlightofthecharacteristicsofitswastewaterquality.Theoperationresultsofthisengineeringprojectshowthattheprocessisreasonableandadvanced;thewaterqualityoftheeffluentcanmeetthefirst-orderof“SewageEmissionStandard”(GB8978-1996).Keywords flavoringwastewater,ABRprocess,hydrolyticacidificationandSBRprocessRESEARCHONPROJECTOFTREATINGWOOLSPINNINGWASTEWATERBYMODIFIEDABPROCESSWuJixiuetal(28)………………………………………………………………………………………………………Abstract Asystematicresearchonthetreatmentofwoolspinningwastewaterbyadsorption-biodegradation(AB)processwasconducted,andtechnicalmodificationsofpretreatmentandABphasewerealsomade.Theworkingprinciple,processflow,designparametersandbenefitofthisprocesswereanalyzedindetailaccordingtotheexampleoftreatingthewoolspinningwastewaterinNO.1WoolenMillofJiangsuJianluCompanyGroup.Keywords woolspinningwastewater,ABprocess,engineeringexampleandresearchEXPERIMENTALRESEARCHONTHEGRAY-WATERTREATMENTBYMEMBRANEBIOLOGICALREACTORWenDonghuietal(30)……………………………………………………………………………Abstract Gray-waterwastreatedbyMembraneBiologicalReactor(MBR).ThebiologicaltreatmentpartoftheMBRsystemwasbiologicalcontactoxidationprocess,andthemembraneseparationpartwashollowfiberUFmembrane.TheexperimentshowedthattheMBRsystemhadtheadvantagesofhighefficiencyandstableoperationinthetreatmentofgray-water.Underthetestconditions,theeffluentcouldmeettheStandardofGray-WaterQuality(CJ25.1-89).Keywords membranebiologicalreactorandgray-waterDEBUGGINGANDSTARTINGOPERATIONOFALARGEANAEROBICREACTORFORHIGHCONCENTRATIONORGANICWASTEWATERLiXiyingetal(32)………………………………………………Abstract Thefullprocessofdebuggingandstartingoperationofalargeanaerobicreactorforhighconcentrationorganicwastewaterispresentedinthispaper.Amediumtemperaturefermentedanaerobicsludgebytreatingthesamesortwastewaterisused,andseedingoffullpotandlowconcentrationisalsoadopted.Loadandtemperaturearegraduallyraised.Enoughhotfermentedactivesludgeiscultivated.Thesystemcanoperatenormallyaftertwomonths,andcostslesstimethantheordinarystartingmethod.3ENVIRONMENTALENGINEERINGVol.20,No.2,April,2002Keywords highconcentrationorganicwastewater,largeanaerobicreactor,debuggingandstartingoperationAPPLICATIONOFMOSSBAUERSPECTROCOPYINTHEEXPERIMENTOFCOALDESULFURIZATIONBYMICROWAVERADIATIONChengRongetal(34)……………………………………Abstract ThispaperpresentstheanalysistotheexperimentofcoaldesulfurizationbymicrowaveradiationwithMossbauerSpectroscopy.Bycontrastwiththeradiatedsampleandtheoriginalsample,dataindicatesthattheisomericshift(IS)andthespectraarea(A)decreaseandthemagnetichyperfinesplittingoccurs,whichshowsthetransformationofpyritetopyrrhotite.O

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